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Dvig učinkovitosti CNC rezkalnega stroja : diplomsko delo Visokošolskega strokovnega študijskega programa I. stopnje Strojništvo - Projektno aplikativni program
ID Marolt, Martin (Author), ID Berlec, Tomaž (Mentor) More about this mentor... This link opens in a new window

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Abstract
V podjetju LTH Castings, d. o. o., se v obratu orodjarne ukvarjajo z izdelavo tlačnih orodij. Na oddelku grobe obdelave CNC stroji, na katerih se izdelujejo sestavni deli tlačnega orodja, dosegajo slabo učinkovitost. Glavni razlog za nizko učinkovitost strojev so pogoste menjave obdelovancev, saj je proizvodnja posamična. Vsaka menjava obdelovanca in nastavitev stroja predstavlja izgube, zato želimo ta čas čim bolj skrajšati. Učinkovitost smo tako izboljšali predvsem s skrajšanjem časa mirovanja stroja med menjavo obdelovanca, kar smo dosegli z metodama SMED in 5S. Z vpeljavo metod vitke proizvodnje nam je uspelo skrajšati čas mirovanja stroja med menjavo za 26,2 % in izboljšati učinkovitost CNC rezkalnega stroja za 11,1 %.

Language:Slovenian
Keywords:vitka proizvodnja, menjava obdelovancev, metoda SMED, metoda 5S, vpenjalni sistemi fast mill, CNC rezkalni stroji
Work type:Bachelor thesis/paper
Typology:2.11 - Undergraduate Thesis
Organization:FS - Faculty of Mechanical Engineering
Publisher:[M. Marolt]
Year:2024
Number of pages:XX, 58 str
PID:20.500.12556/RUL-160840 This link opens in a new window
UDC:658.51:005.935:621.937(043.2)
COBISS.SI-ID:211108355 This link opens in a new window
Publication date in RUL:05.09.2024
Views:151
Downloads:48
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Secondary language

Language:English
Title:Increasing the efficiency of CNC milling machine
Abstract:
The tool shop of the LTH Castings company produces pressure tools. In the rough machining department, CNC machines, manufacturing the components of the pressure tool, achieve low efficiency. The main reason for the low efficiency of these machines is frequent replacements of workpieces, due to an individual production. Every workpiece replacement and machine setting lead to losses, so we want to reduce this time as much as possible. The efficiency was increased mainly by reducing machine downtime during workpiece replacement, which was achieved with the SMED and 5S methods. By introducing lean production methods, we were able to reduce machine downtime during the replacement by 26.2 % and increase the efficiency of the CNC milling machine by 11.1 %.

Keywords:lean manufacturing, workpieces replacements, SMED method, 5S method, fast mill clamping systems, CNC milling machines

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