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Dvig produktivnosti podjetja z metodami vitkosti
ID Zupan, Matic (Author), ID Berlec, Tomaž (Mentor) More about this mentor... This link opens in a new window, ID Kušar, Janez (Co-mentor)

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Abstract
Zaključna naloga obravnava optimizacijo proizvodnega procesa za dvig produktivnosti elektronske antene iz sveta avtomobilske industrije. Pri optimizacij smo se oprli predvsem na načela in metode vitke proizvodnje. Prvi korak izvedbe optimizacije je bil popis obstoječega stanja celotnega proizvodnega procesa. Po končani analizi stanja smo v ekipi zbrali šibke točke procesa in se osredotočili na odprave le teh. Optimizirali smo posamezna delovna mesta in odpravili vsa nepotrebna gibanja operaterja, dvignili smo celotno učinkovitost stroja, ki nam v procesu predstavlja ozko grlo. Celoten potek dela smo organizirali v celično proizvodnjo in poskusili čim bolj optimizirati delovne operacije in enakomerno razporediti delo vseh operaterjev udeleženih v celici. Končni rezultat vseh optimizacij je dvig produktivnosti končnih izdelkov za 28,7 %.

Language:Slovenian
Keywords:vitka proizvodnja metode vitkosti celovita učinkovitost opreme celična proizvodnja uravnoteženje procesa produktivnost
Work type:Final paper
Typology:2.11 - Undergraduate Thesis
Organization:FS - Faculty of Mechanical Engineering
Publisher:[M. Zupan]
Year:2018
PID:20.500.12556/RUL-102958 This link opens in a new window
UDC:005.935:658.5(043.2)
COBISS.SI-ID:16417819 This link opens in a new window
Publication date in RUL:12.09.2018
Views:2230
Downloads:484
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Secondary language

Language:English
Title:Increasing company productivity using lean methods
Abstract:
The present diploma thesis describes the process of optimizing the current manufacture process for increasing the productivity of the automotive keyless-go antenna, with the methods of lean manufacture. The first step was to analyze the current state of the process. After the analysis we pointed out the weaknesses of the current state. We optimized every work place with the intention of eliminating unnecessary movement. We brought up the overall equipment effectiveness of the bottleneck in the production cell. We changed the way of working on every work station indvidualy to working in the work cell. The final result of the optimization was the increas of the productivity for 28,7 %.

Keywords:lean production lean methods overall equipment effectiveness cell production process balancing productivity

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